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Author Topic: Augusta progress  (Read 112448 times)
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Kari
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« Reply #270 on: 16 May, 2021, 09:31:34 AM »

As I have mentioned before, I was wondering how my Augusta would look (and drive) with just one spare wheel. I bought some suitable thin walled tube and made a short stub to replace the original carrier. I have to point out that the boot lid has been modified before I have owned the car. Compared to the original there seems to be a heavier gauge sheet on the inside of the lid. I don't know if this has any influence to the dimesions of the spare wheel carrier. If there is interest to copy the short carrier, I am pleased to pass on the data.
Karl


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Mikenoangelo
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« Reply #271 on: 04 July, 2021, 01:59:08 PM »

Having fixed the things which really needed fixing I don’t have much to report on and am just using and enjoying the Augusta which is proving to be a delightful car and very well suited to the twisting roads around here. I’ll do a recap later of the problems we had and the outcome of the last 18 months of fettling but here is a note on the minor but rather challenging issue of the dreaded fuel gauge.

For those who haven’t come across this, the fuel tank  is mounted under the bonnet above the driver’s knees and connected to the gauge by a cable which is rotated by the gauge sender unit on top of the tank.. The gauge is just a dial with a 270 degree 0-40 litre scale and  a pointer.

The difficult bit is the sender which has to translate the position of a float to rotation of the connecting cable. The translation is done by hanging the float by a fine thread to a small drum about 25mm diameter which incorporates a tiny brass clock spring to tension the thread and turn the gauge pointer and is then geared with a pair of spur gears to the spindle which turns the cable. The cable then passes through a 6mm diameter tube, through the bulkhead to the gauge on the dash. I have the original float, drum and gears but the original casing in which they run, being Mazak, had evidently corroded and had been replaced by a rather crude affair. (Photos 185 and 186).The result was that the device was no longer capable of generating enough torque to turn the cable. I thought  there must be a better way. Others have adapted a modern electrical sender and gauge but I felt that a mechanical setup would be more in keeping.

Most float type gauge senders use a float and lever system but this is not possible for the Augusta as the original float works within the confines of a 62 mm bore vertical tube in the tank. However I found a simple device intended for the fuel tank of an outboard motor and cribbed the idea, adjusting it to suit the tank.  It comprises a metal strip  150mm long x 6mm x 1.5mm which is twisted through 270 degrees to form a very long pitch screw thread. This fits through a cylindrical float, engaging with a slot so that as the float rises or falls, the strip is rotated, the float being prevented from turning by guide rods. The rotating strip is connected by a pair of bevel gears to the cable, and turns the needle of the gauge through 270 degrees as the float moves from bottom to top of its range. The calibration of the instrument is easily altered by increasing or decreasing the twist of the strip. (Photos 187 and 188).

The main problem is that the bevel drive and the connecting cable must be very free to turn and the float free to rise and fall without sticking. The length of the connecting cable is also critical as the distance from sender to gauge is fixed. I used a tongue and fork arrangement at the ends of the cable to provide some tolerance. The float was made from a thick cork bung ( ex Ikea jug!) but could be made by laminating from cork floor tiles. Machined to size 58mm diameter and 42mm high, grooved at either side and  bored through 8.5mm, with a nylon disc at the upper end, slotted to slide on the helical strip, the float’s grooves engage with a pair of 4mm stainless steel rods. The rods hold a lower cross piece with a 5mm hole to form the lower bearing for the helical strip, and their top ends attach to the 80mm aluminium disc which bolts to the top of the tank. A brass fitting was made to carry the bevel gears which are 16 tooth 16mm diameter and run on a 5mm shaft, one end of which forms a tongue to engage with a fork attached to the end of the cable. A gland nut retains the outer tube just as in the original Lancia version. The end float of the  horizontal hear shaft is controlled by a pair of brass collars and the top end of the vertical gear shaft runs in a nylon bush through the top disc. An aluminium cover conceals the gears with just 5mm clearance from the underside of the bonnet top panel.

I made most of the parts in stainless steel and sealed the cork float using a marine grade epoxy resin. Although there  is no guarantee from the supplier that the epoxy will tolerate ethanol in fuel (it is proof against straight petrol) I have used it previously on a cork float fuel sender on a previous project and it was still OK after at least 8 years.

I still have a bit of tweaking to do to get the calibration right but the gauge works perfectly,
the needle being absolutely steady. It does read a few litres high when going downhill, and low going up but on the level gives a true reading.

So rather a lot if time went into the project but it was interesting and satisfying! I’ll add more pictures when I finish calibrating it.

Mike


* 185.Pulley drive sender 1.jpg (109.27 KB, 640x480 - viewed 1015 times.)

* 186. Pulley drive .jpg (101.9 KB, 640x480 - viewed 1036 times.)

* 187. Gear drive.jpg (125.42 KB, 640x480 - viewed 1041 times.)

* 188. Gear dirve with cover jpg.jpg (122.66 KB, 640x480 - viewed 1057 times.)
« Last Edit: 04 July, 2021, 08:28:28 PM by Mikenoangelo » Logged
Raahauge
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« Reply #272 on: 04 July, 2021, 08:37:20 PM »

Well done Mike.
I have taken a different route by trying to recast the original housing in zinc but have so far failed. I am getting closer and with my improving skills I think my next attempt might be a success.
The old unit had, apart from the common problem of distortion and cracking with ageing pot metal, been soldered into the recess in the tank and it was quite difficult getting it out.
The mechanism is attached to the flange at the top of the 62mm tube mentioned by Mike and the outer diameter of this flange is soldered to the underside of the roof the tank to seal it. This solder joint had failed causing a leak leading to some previous owner's expedient repair of soldering everything up. I mention all this to alert you, and anyone else, to the possibility that any leak you may have may be from this joint.


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Mikenoangelo
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« Reply #273 on: 06 July, 2021, 09:05:15 PM »

It seems the main problem with the original fuel gauge setup is the need to get just the right combination of float buoyancy and tension in the small hairspring to overcome the friction of the cable rotating in the tube connecting sender to gauge. Perhaps a better plan would be to simply put a pulley at the top of the tank sender unit, extend the connecting thread, and move the rest of the mechanism to a point at the back of the gauge behind the instrument panel. Hindsight is a wonderful thing!

Mike - I never tried foundry work although I have made a few simple patterns. An interesting challenge but you will still have some machining to do. I wonder why you are using zinc rather than tossing a few old aluminium pistons into the pot? My fuel sender also leaked a bit around the rim as you can see from my photo but this was due to a poor gasket and stripped threads in some if the retaining screws. It does look as though some soldering has been done around the rim.

Mike
« Last Edit: 06 July, 2021, 09:07:57 PM by Mikenoangelo » Logged
Raahauge
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« Reply #274 on: 11 July, 2021, 08:43:48 PM »

Mike.
Foundry work is very satisfying in a sort of basic way and also interesting because it is outside my general experience.
The use of Zinc is part of my improving skills and part of the learning process. I started with scrap aluminium but the sections are very thin and I couldn't get it to flow well enough. I am optimistic (hoping) that I will not have to machine it apart from drilling some holes.
It has consumed a stupid amount of time thus far!





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Mikenoangelo
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« Reply #275 on: 13 July, 2021, 08:42:34 PM »

Now I’m down to the details - an annoying but minor rattle from a rear door led me to investigate the latch plates on the body for the top of the doors. These are another example of Lancia’s attention to the finer points. As mentioned in an earlier post the latch plates actuate the retractable sprung latches on the doors as they are closed but also incorporate rubber buffers for the doors and are themselves also rubber mounted  and able to turn to align with the closed door. They appeared to a bit loose because their rubber mounting bushes were perished and their fixing bolts loose. Luckily I had a sheet of 4mm rubber which when wrapped around the metal centre sleeve and pushed into the outer housing made a reasonable bush so that now the doors close and the rubber takes up any slop. Rattle gone!.

It took a day’s fiddling, as to get at the mounting bolts involves lifting the trim panels above the door which in turn requires removal of the panel above the windscreen, the mirror and the sun visors. All of these are fixed with 4mm screws which pass through a wooden filler behind the trim and into holes drilled in the inner body panels around the doors and windscreen. The wooden filler panels are a work of art rather than the usual scrap of hardboard! They are machined to incorporate various recesses and fit to the metal body frame. Interestingly the bolts (more like self tapping screws) which hold the latch plates are 5/16 inch and have half inch A/F heads, perhaps American origin.

Mike
« Last Edit: 14 July, 2021, 07:00:09 AM by Mikenoangelo » Logged
Mikenoangelo
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« Reply #276 on: 23 July, 2021, 08:29:13 PM »

More experience with the helical drive of my geared fuel tank sender (Photo 189) showed that despite the epoxy coating, the cork float absorbed fuel over a week or so and messed up the calibration. The float grew in diameter by 3mm and so stuck on the guide bars. I bought an ethanol proof SU float from Burlen and was able to use a metal bridge piece across the top of the float to engage with the two side rods to stop the float rotating and it now seems to work very well without sticking. I must say the reading is much affected by the gradient of the road and possibly needs  a slight reduction in pitch of the helical bar to match the fuel level shown on my dipstick. One issue I noted was that it is essential to have a little end float to the connections at either end of the thin connecting cable from sender to gauge as any end loading puts a wave in the cable which make it bind in the guide tube.

I am now reduced to working on the only remaining known issue - rebinding the braided grab handle for one of the rear seat passengers! A job more suited to the denizens of “The Repair Shop” on TV! Of course as once famously said there will be unknown issues which I don’t yet know about, but so far I can’t see anything else which needs fettling.
Mike


* 189 Fuel gauge float and helical drive.jpg (113.74 KB, 640x480 - viewed 927 times.)
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neil-yaj396
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« Reply #277 on: 24 July, 2021, 07:44:02 AM »

Great that you have overcome all those niggles Mike. Often, owners, especially those not using their cars so much, just put up with them.
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1979 1300 Beta Coupe, 2014 Ypsilon 1.2 S Series Momo
Mikenoangelo
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« Reply #278 on: 02 August, 2021, 08:15:07 PM »

 Neil - I like fettling just as much as driving and I must say that during lockdown and two salty winters it's been a much appreciated challenge and learning experience.

Having now done about 2000 miles with the Augusta I thought a few comments on the success or otherwise of my fettling activities might be in order.
I bought the car from Italy, mainly on the basis that it is in very nice, sound bodily condition and was from long term ownership by an enthusiast who had recently passed away. There was no opportunity to really assess its mechanical condition which turned out to have a number of issues, fortunately none too serious. Mechanical problems are more easy to solve than bodywork issues.

The most trying problem was vibration which has taken a lot of effort to cure. The culprit was, as I first thought, the propshaft. After being sidetracked by having it professionally (but badly) balanced, which seemed to make no difference I replaced the fabric discs and centerng spiders and eventually worked out a way of balancing the whole unit by supporting it  on two level bars on which the centering spider bosses could roll. A Jubilee clip and a small piece of lead resolved the issue.

There were also vibrations from the engine, significantly reduced by replacing coil, points condenser and plug leads, grinding the valves and getting the mixture right. I had not understood that the two leaf springs which support the engine bearers also incorporate a vibration damper in the form of strips of brake lining between the leaves. One side was seized and the spring leaf surfaces covered with solid black gunge whereas on the other side the leaves were polished. Sorting that out greatly reduced engine vibrations to an acceptable level. The carburettor (Weber DO) suffered from a worn slow running jet and seat which I remachined, greatly improving the carburetion as confirmed by readings on the Air /Fuel ratio gauge I fitted. Subsequent experience shows that the carburettor is as it should be since the A/F ratio fluctuates around 13.5 to 1, dropping to about 11.5 to 1 when pulling hard uphill. One curious feature of the carburettor is that the choke can be used to enrichen the mixture when pulling with the throttle wide open - this works and the A/F ratio goes down to 10 to 1 with a small but detectable increase in power.

I had the cylinder head re-faced and ground the valves, fitting a modern oil filter and rebuilding the water pump with a new stainless steel impellor shaft but re-using the original rope gland.  I improved the water flow to the rear corner of the head/manifold and made a simple copper “heat exchanger” to replace the exhaust flange gasket with the aim of drawing more heat out of that corner of the head. This does seem to help as there is only a slight degradation of the paint at this point after 1000 miles. I sealed the flange joint using “Heldite” sealant which has worked well in sealing this unit of three plates of 3mm copper but no gasket. The engine is now leak free,  starts immediately from cold and runs with no flat spots or stalling when braking to a standstill. It had been rebuilt by the previous owner with a crank regrind, rebore and new pistons and cranking by hand tells me that the compression is excellent. It runs about 1000 miles on a litre of oil and does not smoke either on starting or after a steep descent. The modern oil filter leaves the oil clean on the dipstick for at least 1000 miles.

The gearbox needed a full rebuild with new bearings and attention to wear on the front end of the input shaft and at the front of the main shaft. The freewheel was very worn but, thinking that I would probably not use it I decided to remove it altogether rather than tackle the worn parts. With the gearbox out of the car I discovered that the large coil spring of the clutch was very much out of true and would not sit squarely in the recess. A new spring was fitted. None of these gearbox or clutch jobs made the slightest difference to the vibration, or even to the characteristic growl of second gear! The clutch did not need relining and with the new spring is smooth to engage and does not slip. It’s a delightful box to use - who needs synchromesh!
 
I abandoned he curious float and string operated fuel gauge sender and made a new unit utilising a helically twisted metal strip which is turned by an adapted modern E10 proof float and connects via a small pair of bevel gears and cable to the gauge. This works .

Two more major tasks were involved. The front suspension was filled with grease so had to be dismantled to clean and check. It turned out that some of the minute sprung loaded valves  were coil bound on their closing springs so hardy surprising that it bounced and clattered. All is now in order although it does still drip oil from bottom of the sliding pillars.

The final major task was to rebuild the rear friction shock absorbers whose wooden discs were worn very thin. I replaced these with new discs laser cut from thin oak and reassembled the units which are preloaded with a coil pressure spring, changing this for an Andre Hartford style star spring and adjusting nut. The links connecting the arm to the axle were remade to a more machinist friendly design with polyurethane bushes. The shock absorbers appear to work satisfactorily but made an annoying creak at low speeds when greased with normal grease but this was cured by using molybdenum disulphide CV joint grease on the discs. I replaced the front eyebolts and all bushes on the rear springs and fitted new brake cylinders as these were scored and tended to seize.

Of course there were many more small jobs done but I finally have a very useable, nippy little car with superb road manners which makes other cars seem clumsy. I have really enjoyed fettling the car, the design of which is so different to other makes, sometimes eccentric, but mostly very effective and full of character. I am now making every excuse to use it and enjoying that too.

I don’t have much more to report having gone through almost every part of the car with the exception of the rear axle (which touch wood seems to be in good order and reasonably quiet. Hopefully these are last words but not famous last words!

I’d like to say many thanks to all those who have advised and helped me over the last couple of years and to thank you all for your interest in Augusta Progress.

Mike
« Last Edit: 02 August, 2021, 08:20:35 PM by Mikenoangelo » Logged
Charles
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« Reply #279 on: 13 August, 2021, 07:15:25 AM »

Bravo indeed, what an inspiring tour de force.
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Augusta berlina, Appia S3 berlina
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nevillesponge
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« Reply #280 on: 15 August, 2021, 09:04:50 PM »

Hi Mike,
Although only an Augusta (well, Belna actually) owner for around a year, I’ve found your articles so very helpful. Your passion and expertise will undoubtedly keep a few more cars on the road.
Thanks and kind regards
David
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Mikenoangelo
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« Reply #281 on: 18 August, 2021, 08:34:24 PM »

Thanks David - I try to keep a diary of work I do on my cars so writng it up is not much of a chore. Glad you appreciate it!

Another small problem fixed. A few months ago the oil pressure fell so I cleaned the piston of the pressure relief valve which lurks behind a very difficult to remove domed, slotted plug in the side of the cylinder block just behind the water pump. This cured the problem so other than making a new hex head plug to improve access I left it at that. However yesterday the pressure dropped again so I had another look, discovering that the conical valve surface of the spring loaded piston was worn and evidently could seat itself badly in the valve. A few minutes in the lathe (Photo 190) sorted that out and the oil pressure is now back as it should be, well over the midpoint of the gauge at 2000rpm

A useful tip:-  after the plug is unscrewed and the spring has been removed from the valve, the piston usually stays behind in the valve so I keep a piece of plastic tube to push into the piston to help pull it out. With the hexagon plug and this piece of plastic the job could easily be done by the roadside if needed, otherwise with the original slotted plug it would be a workshop job.

Mike


* 190.Oil pressure relief valve piston with worn conical tip.jpg (73.59 KB, 640x480 - viewed 687 times.)

* 191. Pressure relief valve after refacing the tip ..jpg (92.76 KB, 640x480 - viewed 670 times.)
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daniel.bangham
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« Reply #282 on: 02 November, 2021, 08:32:03 AM »

Thank you for your posts, they are very helpful and interesting. I am about to overhaul the sliding pillars on my Belna and would rather borrow/hire the tools needed, rather than make a new set. I met a lovely and enthusiastic gentleman at the rally, who's name I have forgotten, that offered to lend me his, so if he or anyone else has a set for hire, please let me know. Daniel Bangham . Cambridge.
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Mikenoangelo
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« Reply #283 on: 02 November, 2021, 10:54:24 AM »

Daniel I've emailed you. You are welcome to borrow my pillar tools (as on the first post on this thread).

Cheers Mike
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daniel.bangham
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« Reply #284 on: 28 December, 2021, 04:33:42 PM »

Good to hear of progress, I did my front suspension a few months ago.
Both had water in them and as a consequence some rust. The damper rods were serviceable but one of the smaller damper drive springs was broken and the other rusty so had some more made, available if you need any.
The water was there because the upper dust cover was absent. The top cap has about a 12mm hole and the damper rod is 10mm. so nothing to keep the spray out.
I have not been able to find out what the original arrangement was, would be interested to know what you have. I have made a couple of push-on covers.

Hi Raahauge
I have just taken my Belna suspension apart and found spring number  34-5583/6 has broken. Is this the one you had made. It is middle spring of the trio on the top section of the suspension. I also had to remake the oil cap/cup found at the very bottom of the suspension. The existing ones have been soft soldered in place, does anyone know if that was the original method of attachment. (part number 34-5595) The original caps are pressed steel with oil tube brazed in place. I have machined the new ones out of free machining mild steel and then re brazed the original oil tube. That way I did not have to cut the very fine thread for the retaining cap.
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